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The launch on the first run didn’t seem all that spectacular as I pulled the front wheels probably about a foot and a half and didn’t really feel that “dead hook” sensation that lets you know you're glued to the track. The car pulled strong to the finish and I figured I may have run a high 11.30 but wasn’t expecting much. When I got my time slip I saw I had actually had a 1.502 at sixty feet but HOLY COW I went 11.267 at a whopping 117.38 mph! Man I’m telling ya it didn’t feel THAT fast! I ran the car across the scales and I was in at 3190 lbs. against my minimum of 3170 lbs.

The only thing I noticed that wasn’t right was that the alternator belt made a loud squeal when I started the engine and I could hear it squeal when I revved up the engine slightly. I thought “here we go again.” It seems if I’m going to have a problem it more than likely will be at Earlville. Back in the pits myself and buddy Jim Kramer looked things over and checked the voltage of the battery only to find it really low and not charging up very fast to boot. I figured I had broken a plate in the battery and it was grounding out.

Luckily fellow racer and all around nice guy Greg Anderson (not THAT Greg Anderson), had a spare battery that would fit and offered to let me borrow it. The only stipulation of course was that if we ended up in the finals together he wanted his battery back! I promised him it was a deal and installed the new power producer and was ready to go. Second round of qualifying was called and I headed eagerly to the lanes hoping to come close to duplicating the first run as the weather was now at about 2300 ft.

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This is where things got interesting and FUN! I’m not sure if it was the track “coming in" or the new juice from the battery or just the stars in alignment, but I knew as soon as I launched this was a DEAD HOOK! The Muscrate pulled the biggest WHEELSTAND ever and all I could see was SKY! I’m sure as the front end was coming down I must have had the biggest smile on my face ever seen on a man in a helmet!

When the front landed the car choked up quite bad from what I imagine was fuel slosh and then rocketed down the track. I thought to myself “man, if THAT wasn’t a 1.40 sixty foot I don’t know what is!” I eagerly accepted my time slip and all I could say was “Holy S**T”!!! I had gone a 1.443 in the sixty foot!! The ET wasn’t much better due to the stumble but it was a fine 11.25 @ 117.58 mph. I’m telling you I could have gone home a happy man at that point, but I figured as long as I was there I might as well take home some money.

My first round opponent had an “issue” after his burnout so I had a single and had a 1.48 sixty foot and ran 11.31 @ 116.85. The squealing alternator belt was back again and would continue to haunt me the next couple rounds. I hadn’t qualified #1 but I was the fastest car in the race. For me this was great, as I consider it to be a whole lot easier to do the chasing.

Second round opponent Richard Myers and his 14.00 second U/SA Mopar wagon gave me a real close race as I had him slightly on the tree and I ran an on-the-brakes 11.311 on a 11.31 dial to his 14.055 on his 14.05 dial. True win was .012". A couple of weeks before at the bracket races I had won a round by .0003”, that’s 3 TEN thousandths! I also lost in that race by a stinking thousandth! So a hundredth was no big deal, yeah right!

The next round was the finals and guess who was in the other lane? You guessed it, Greg Anderson. He jokingly requested his battery be returned and I agreed to return it after the finals. Not much good to tell about that race as I had a horrible reaction time and Greg gladly handed me my ass on a platter for the win.

Over all, it was a really good day at the races and I went home with a warm fuzzy feeling in my stomach for a couple of reasons. First, I had a 1.44 sixty foot! Second, I had some fun which has been a long time coming. Third, I am completely confident that if nothing goes catastrophically wrong between now and October I WILL see a 10 second time slip.

Considering about a month ago my index was 12.35 I feel I’m on track to see the performance I estimated was possible when I first switched to this combination and boldly (perhaps stupidly) predicted I could go tens with a “Stocker” FORD 302. I may be wrong, but I am not aware that has ever been done before?

In closing, I will say that I am very impressed with HUGHES PERFORMANCE and they will get more of my business in the future. My charging problem ended up being a bad bearing in the alternator so hopefully I can get a hold of one of MSD's new billet racing units and end the problem. I’m going to do some more testing in the following weeks and some more racing so be sure and check back next month to see what kinda trouble I’ve gotten myself into! Until then remember, there’s always hope and….

…When in doubt… DO A WHEELIE !!! A really BIG Wheelie!!!

SOURCE
Hughes Performance
2244 West McDowell
Phoenix, Arizona 85009-3009
(602) 257-9591
www.hughesperformance.com

Project Muscrate [7-8-05] We can rebuild it! We have the technology!









 
 

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